Anatomy of a Tragedy
On March 23, 2005, tragedy struck BP’s Texas City, Texas, refinery when a cloud of hydrocarbon vapor exploded, killing 15 workers and injuring more than 180 others. Perhaps the real tragedy is that federal investigators believe that the accident – like so many other workplace accidents – was entirely avoidable.
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Time after time, those of us in the safety community read about
workplace injuries and fatalities that were completely preventable.
“Had Company X just followed basic workplace safety
requirements,” the investigating agency often concludes,
“this accident never would have happened.”
Tragically, the March 23, 2005, explosion and fire at BP’s
Texas City, Texas, refinery – which took the lives of 15
workers, sparked the largest investigation in Chemical Safety and
Hazard Investigation Board (CSB) history and created a public
relations nightmare for London-based BP PLC – was just such
an accident.
With the release of CSB’s final investigation report on
the root causes of the BP refinery tragedy, as well as with the
previous releases of the independent Baker panel report and
BP’s own investigation report, the safety community now has
unprecedented insight into the decisions and actions that
precipitated the worst U.S. industrial accident since
1990.
The body of evidence and information available to the safety
community – and to the public – is the anatomy of a
workplace tragedy that never should have happened. It is the
anatomy of a tragedy that, in the words of CSB Chairwoman Carolyn
Merritt, was “the inevitable result of a series of
actions” by BP.
Technical Cause Not in Dispute
By now, there’s little dispute over what happened in the
hours leading up to the accident. During a startup of the
refinery’s isomerization unit, operators pumped flammable
liquid hydrocarbon into the raffinate splitter tower without
allowing any liquid to drain from the bottom of the tower into
storage tanks – which was contrary to startup
procedures.
The liquid overflowed into piping off the top of the tower,
triggering emergency relief valves to open. The emergency valves
channeled liquid hydrocarbon into the blowdown drum at the other
end of the isomerization unit.
In the 6 minutes that the emergency relief valves were open, CSB
estimates that 51,900 gallons of flammable liquid flowed from the
raffinate splitter to the blowdown drum.
The drum filled completely, and, consequently, liquid
hydrocarbon spewed from the 113-foot tall blowdown stack like a
geyser. Although the eruption only lasted about 1 minute, CSB
estimates that the blowdown stack released 7,600 gallons into the
atmosphere.
The volatile liquid hydrocarbon evaporated as it fell to the
ground and created a large flammable vapor cloud, which spread
quickly throughout the area. At 1:20 p.m. on March 23, 2005, the
cloud ignited, likely after coming into contact with an idling
diesel pickup truck parked about 25 feet from the blowdown
drum.
According to BP’s modeling and other calculations, the
ignition of the vapor cloud created a fireball with a diameter as
large as 236 feet. BP estimates that the fireball lasted 6
seconds.
Extensive Destruction
CSB and BP agree that the 15 contract employees killed in the
explosion were working in or near mobile trailers located too close
to the blowdown drum. Many of the injured also were in or near
these trailers, which were used for supporting turnaround work on
the nearby ultracracker unit.
The explosion caused heavy damage within the isomerization unit,
severely damaging the satellite control room and destroying the
catalyst warehouse. The blast damaged or destroyed a number of
vehicles and mobile trailers near the isomerization unit.
The explosion also damaged more than 50 large chemical storage
tanks – many located more than 250 feet away – and
broke windows, cracked masonry walls and damaged doors in
surrounding units of the refinery.
Off site, the blast shattered windows in homes and businesses up to three-fourths of a mile away from the isomerization unit.
One Key Mistake?
While BP’s final investigation report admits that there
was a complex set of “underlying reasons for the behaviors
and actions during the incident,” the report clearly
emphasizes that workers and supervisors caused the accident by
deviating from procedures. The BP investigation team asserts that
one key mistake “was instrumental in leading to the
incident.”
That mistake was the failure of BP personnel – both the
night shift on March 22 and the day shift on March 23 –
“to establish heavy raffinate rundown to tankage, while
continuing to feed and heat the tower.”
During the day shift, BP operators pumped 20,000 bpd (barrels
per day) of liquid hydrocarbon into the already-full raffinate
splitter tower for approximately 3 hours without any egress. When
they finally did begin to send liquid out of the tower to storage
tanks – just minutes before the accident – it was too
little, too late.
“If a heavy raffinate rundown flow had been started as
soon as the feed was re-established, the incident would not have
occurred,” the BP investigation team wrote. “The
absence of supervisory presence on the unit probably contributed to
the failure to establish rundown.”
Underscoring BP’s emphasis that workers shoulder much of
the responsibility for the accident, the Houston Chronicle
reported that BP, in the wake of the 2005 accident, fired six Texas
City workers. BP spokesman Neil Chapman would not comment
specifically on the firings but acknowledged that the company
“took disciplinary action against both supervisory and hourly
personnel.”
“The actions did range from dismissals to warnings, and really that’s all we can say about personnel matters,” Chapman told OCCUPATIONAL HAZARDS.
Problems “At All Levels”
The BP report acknowledges that Texas City had a broken safety
culture. However, the report traces the roots of Texas City’s
safety dysfunctions – which ranged from poor hazard awareness
to high risk tolerance (regarding the latter, BP’s
investigation team observed that Texas City workers believed that
“fires were a fact of life in the refinery”) –
only as far up as Texas City management.
In contrast, CSB emphasizes that the accident “was caused
by organizational and safety deficiencies at all levels of the BP
corporation,” and that many of those deficiencies can be
traced back to decisions made by BP executives in London.
“The BP chief executive [Lord John Browne] and the BP
Board of Directors did not exercise effective safety
oversight,” the CSB report states. “Decisions to cut
budgets were made at the highest levels of the BP Group despite
serious safety deficiencies at Texas City.”
Noting that the Columbia Accident Investigation Board concluded
that NASA’s organizational culture and structure had as much
to do with the 2003 space shuttle Columbia disaster as the
immediate cause did, CSB points out that its investigation of the
Texas City accident was conducted from a similar
perspective.
“Simply targeting the mistakes of BP’s operators and
supervisors misses the underlying and significant cultural, human
factors, and organizational causes of the disaster that have a
greater preventative impact,” CSB’s report
says.
It Started at the Top
After BP and Amoco merged in 1999, CEO Lord John Browne mandated
a 25 percent across-the-budget cut in fixed spending at the
corporation’s refineries, “even though,” CSB
points out, “much of the [Texas City] refinery’s
infrastructure and process equipment were in disrepair.” In
late 2004, BP refinery executives issued a 25 percent budget
reduction “challenge” for 2005.
Budget cuts thinned Texas City’s operator ranks, reduced
the refinery’s training budget, downsized the training staff
and impaired mechanical integrity. According to CSB, cost
considerations scuttled attempts to replace the blowdown drum
– which was installed in the 1950s and, the BP report admits,
was not intended “for emergency use during, for example, a
relief event.”
Ultimately, CSB concludes that “cost cutting and failure
to invest in the 1990s by Amoco and then BP left the Texas City
refinery vulnerable to a catastrophe.”
Meanwhile, BP executives’ fixation on injury rates –
which were improving – gave them a false sense of security
regarding the conditions at the refinery.
“BP Group executives used personal safety metrics to drive
safety performance,” the CSB report says. This over-emphasis
on personal safety “helped mask severe shortcomings in
process safety.”
Even so, CSB asserts that top executives “received numerous
warning signals about a possible major catastrophe at Texas
City.”
“Numerous surveys, studies and audits identified
deep-seated safety problems at Texas City,” CSB says in its
report. During the March 20 unveiling of CSB’s final report,
CSB lead investigator Don Holmstrom told reporters: “These
audits and studies were shared with BP executives in London and
were provided to at least one member of the executive
board.”
Holmstrom acknowledged that BP officials tried to improve the
conditions at Texas City from 2002 to 2005, but their efforts were
focused on personal safety goals such as preventing slips, trips
and falls “rather than than on the big picture: improving
process safety performance, which continued to
deteriorate.”
If BP executives had wanted to put their finger on the pulse of
the safety risks at Texas City, they needed to look no further than
history: In the 30 years prior to the 2005 disaster, there were 23
worker deaths at the refinery – three of them in
2004.
Damning Documents
BP disputes CSB’s assertion that “[b]udget cuts and
production pressures seriously impacted safe operations at Texas
City.”
Chapman pointed to page 143 of BP’s report, which states
that the Texas City budget for capital expenditures averaged less
than $50 million per year from 1996 to 2000 but increased to an
average of $125 million per year from 2001 to 2004,
“primarily for investment in clean fuels and other
environmental projects.” According to the BP report, fixed
cash costs increased in 2004 and spending on maintenance
turnarounds increased from 2001 through 2004.
“So when looking at this incident, budget did not appear
to play a role,” Chapman told Occupational Hazards.
CSB, however, determined just the opposite. While Holmstrom
acknowledged that BP had increased its maintenance spending at
Texas City in recent years before the accident, he said that
“we found the increases were largely spent complying with
environmental requirements and responding to repair major accidents
and outages.”
And when CSB unveiled its final report, it also released about
20 damning internal BP documents that corroborate the
agency’s assertion that budget cuts played a role in the
Texas City disaster. These documents offer a rare inside glimpse of
a workplace where, in hindsight, a serious accident was just
waiting to happen.
A 1999 e-mail from Texas City management explained that
Browne’s top goals for the company included reducing the
days-away-from-work rate, reducing CO2 emissions and
“reduc[ing] business unit cash costs for the year 2001 by at
least 25 percent from 1998 levels.” The e-mail did not
mention process safety management.
The e-mail added that Texas City’s strategy to meet
Browne’s cost reduction goal was to “continuously and
aggressively drive costs out of the system at an accelerated pace
relative to other refiners.”
“Items cut included turnarounds; safety committee
meetings; the central training organization; fire drills;
maintenance, engineering, supervision and inspection staff; plant
maintenance; and training courses,” the CSB report explains.
“Safety and maintenance expenditures were a significant
portion of the cuts.”
In 2004, researchers from the consulting firm Telos Group
surveyed 1,080 employees and interviewed 112 as part of a safety
culture assessment of the refinery. In a confidential executive
summary dated Jan. 21, 2005, the consulting firm points to the
connection between budget and production pressures and safety
problems at Texas City.
“Most interviewees at the production level say that the
pressure for production, time pressure and understaffing are the
major causes of accidents at Texas City,” the executive
summary states. “They say all of these have gotten steadily
worse in recent years and that cuts have gone beyond what is safe
in many cases.
“ ... Most interviewees say that production and budget
compliance gets recognized and rewarded before anything else at
Texas City.”
The Telos Group concludes: “There is an exceptional degree
of fear of catastrophic incidents at Texas City.”
Another red flag appeared in the 2005 EHS business plan for the
refinery. The document prophetically stated that the key risks for
2005 included the possibility that the Texas City refinery
“kills someone in the next 12 to 18 months.”
“Ripe for Human Error”
While BP asserts that a failure to follow procedures caused the
Texas City tragedy, CSB contends that “safety system
deficiencies created a workplace ripe for human error to
occur.”
Due much in part to production pressures, a crumbling
infrastructure and budget cuts, “numerous latent conditions
and safety system deficiencies at the refinery influenced
[operators’] actions and contributed to the
accident.”
According to the CSB report, the work environment at Texas City
encouraged BP employees to deviate from procedures. Consequently,
the agency believes that the deviations on March 23, 2005,
“were not unique actions committed by an incompetent
crew” but instead were actions that “operators, as a
result of established work practices, frequently took to protect
unit equipment and complete the startup in a timely and efficient
manner.”
“Indeed, several procedural deviations made by the
operations crew on March 23, 2005, were common practices in 18
previous raffinate splitter tower startups,” the CSB report
says.
The unit’s malfunctioning instrumentation kept personnel
in the dark regarding the volatile situation brewing in the
raffinate splitter tower. CSB points to a level transmitter that
indicated that the liquid level in the tower was gradually
declining when it actually was rising; a redundant high-level alarm
that failed to activate; and the tower-level sight glass, which
“could have provided a visual verification of the actual
tower level” had it not been “dirty and
unreadable.” The report adds that the sight glass “had
been nonfunctional for years.”
“When instrumentation provides false or misleading
information,” CSB says, “accidents are
likely.”
BP’s lack of a fatigue prevention policy was another
underlying latent condition. BP admits that some employees in the
isomerization unit, prior to the accident, had worked up to 30 days
of consecutive 12-hour shifts. The company, however, says it cannot
“directly attribute actions or inactions of the operators and
supervisors to fatigue.”
CSB disagrees. The agency asserts that BP personnel involved in the
accident demonstrated telltale signs of fatigue.
“The board operator, as well as the outside operators, did
not recognize that feed was entering the tower but not being
removed from the unit for 3 hours, that the tower was overfilling
or that the consequences of the tower flooding might be
catastrophic,” the CSB report states.
“ ... It is common for a person experiencing fatigue to be
more rigid in thinking, have greater difficulty responding to
changing or abnormal circumstances and take longer to reason
correctly.”
Other underlying latent conditions, according to CSB,
included:
- A poorly designed computerized control system that hampered the
ability of operations personnel to determine if the tower was
overfilling.
- Insufficient staffing to handle board operator workload during
the high-risk time of startup.
- Inadequate operator training for abnormal and startup
conditions. From 1998 to 2004, BP Texas City’s training
budget had been cut from $2.8 million to $1.4 million and the
training staff had been reduced from 28 people to eight
people.
- Lack of a BP policy on effective communication for shift change
and hazardous operations such as unit startups.
- Concludes the CSB report: “The broader aspects of this
investigation revealed serious management safety system
deficiencies that allowed the operators and supervisors to
fail.”
“A Very Different
Company”
Despite voicing “strong disagreement” with some of
CSB’s conclusions, BP clearly has been chastened by the Texas
City accident.
The company said it expects to invest more than $1 billion over
the next several years to improve safety processes and equipment at
Texas City. According to BP, the changes it has made or is making
encompass “600 recommendations and 1,000 specific actions
based on findings from BP’s internal accident investigation
team, OSHA and other external organizations.”
According to BP, those changes include:
- Leadership development and other training programs that will
involve a projected 300,000 training hours each year.
- Isolating or removing all blowdown stacks and installing a new
flare system.
- Removing more than 200 temporary structures from the
site.
- Introducing a sitewide transit system to reduce the number of
vehicles allowed within the refinery.
- Initiating a stop-work program for startups.
- Requiring supervisors to be present for all startups, shutdowns
and other critical operations and requiring written shift handovers
with supervisors present.
- Appointing former U.S. District Judge Stanley Sporkin as an
“ombudsman” to investigate employee safety
concerns.
Demonstrating BP’s desire to repair the refinery’s
safety culture, Chapman noted that Texas City Refinery Manager
Keith Casey visits with employees before every unit startup, looks
them in the eye and asks them, ‘Is it safe to start this unit
up?’”
“People have raised issues at that point and seen action
being taken,” Chapman said. “And that speaks
powerfully.”
As for CSB’s most recent batch of recommendations (see
sidebar for a list) Chapman said that BP is reviewing the CSB final
report “and seeing how we can integrate their recommendations
into the actions that are already being taken.”
CSB’s Merritt expressed confidence that BP will
“address all of the issues that have been identified in our
report as well as in their own internal investigation.”
Merritt added: “BP is going to be a very different company as
a result of this investigation and as a result of this
incident.”
Chapman agreed.
“It’s echoed from our senior management all the way
down to almost everybody you meet throughout the company: This is
an event that has changed the company, and the commitment to safety
has been reinvigorated,” Chapman said. “People were
absolutely shocked by what happened. They were shaken by what
happened. Fifteen people lost their lives, and our company has
changed forever. Inside the company you can see it, because the
reinvigoration and the focus on safety is so
strong.”
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© 2012 Penton Media Inc.